I got one routine project completed and that is the annual maintenance on our Aqua-Hot system. It is what provides continuous domestic hot water and coach heat. It uses two electric elements and a diesel burner. Every year the manufacturer recommends changing the diesel fuel filter and the burner nozzle, a check of components and a cleaning of the combustion chamber, sounds like a lot but it takes only about an hour. And even better, in our coach, the unit is right inside a basement door and very easy to access.
Easy access |
Ready to remove the burner |
Cleaning out the combustion chamber |
The nozzle ready to be replaced The flame sensor and fire rings ready to be cleaned |
Soon to be reassembled |
The rest of the projects were completed with the welcome help of friends, without whom Jan and I might still be working on them. It is so very nice to be surrounded with exceptional people who are ready to jump in at any time and lend a hand. We are very fortunate, and in those few times when Jan and I think about maybe spending our winter elsewhere, it is our friends that keep drawing us here.
First up was running a new wire to provide power to our small air compressor that I have mentioned many times that provides air to keep our coach level when we are using our air leveling system as opposed to hydraulic jacks. We have had an abundance of issues with it since we got our coach and each time we think we have solved the problems we are bit with another, in fact, that once again happened this time. Originally they had mounted the compressor up in front of the drive axle, completely open to the weather and road dust, mud, and grime. It would often clog up the compressor and played havoc on the pressure switch which turns it off and on. We had moved its location to a basement to keep the compressor out of the weather, and it had operated flawlessly for several years.
The new location in 2015 |
Jan and Harold deep in the basement |
This is the Front Run Bay where most of the 12 volt power and fuses live The new black wire is coming from the top of the compartment |
Harold getting the wire through the difficult wheel well area |
The next one on the list was the skid plates under the rear passenger side slide and replacing the bottom seal, and again it was the help of friends that got the job done. First I had to jack up the slide a bit and needed a 4X4 the right length, so Scott said he knew where one was and promptly took me on a golf cart to get it. Got it cut to length and we were in business.
Harvey watching, Scott holding, me cutting, and Harold holding |
Scott, Harold, and I jacking up the slide |
You can see a hole on the metal flange where the seal fits, and also see the marks on the bottom of the slide where the rollers are wearing |
Our workbench with a skid plate almost ready |
Applying some silicone |
Harold and I mounting the plate |
A view inside of the roller without the plate |
And with the plate |
Harold and I working on the tape |
Tape ready for the seal |
Seal installed |
Here you can see the skid plates and the new seal |
The last challenge was what we thought was a no-brainer and easily done, we couldn't have been more wrong. Our coach has a articulating door on our plumbing and electrical bay that gets it up and out of the way unlike a swinging door. It is assisted in its movement by 2 gas struts.
Closed |
Open |
This shows one of the 2 struts |
Now I felt like the door was getting harder to raise and figured the original struts were getting tired, so I ordered 2 new struts using the part numbers on the original struts. Easy-peasy, right? Wrong. I got the struts and went to line them up to make sure they were correct and they were too long, by about an inch. Now I should mention that these struts are powerful, even though these are rated 35#, you cannot compress them manually, you can stand on them, lean on them, and they do not move a millimeter. So we figured they were the wrong strut after all, so in order to be sure, we pulled off one of the "bad" struts, and as it sprung off, we lined it up against the new one and they were exactly the same. Now what? Now we can't even get the original strut back on!!! Well, Harold and I, and eventually several others tried every which way to manipulate the hinges and the door, and finally removed the door, and each end of the arms to see if there was a trick to getting them on. If there is, we never found it, how Monaco ever got them on is beyond us.
We had lots of help and opinions too. Harvey, myself, Harold, Bob, and Joe all trying to figure out the puzzle |
Damn, it has to work somehow. |
I went over the next day and he and Scott were sitting there working on a custom tool Jack had invented, then by using Harvey's large pipe clamp to compress the strut, we inserted the strut in the tool, and used vise grips to amazingly hold the strut compressed, it left the attachment clips accessible for putting it on the door. After 3 or 4 attempts to get everything in exactly the right place to go on the door, it went right on! The first one took maybe 30 minutes for the learning curve and the 2nd one took 3 minutes, and he even gave me his custom tool so I would be able to do it myself if I ever have to replace them again.
Jack, me, and Harold with success! |
A long post, but we got a lot done. Our to-do list is almost whittled down to nothing now. A few more way simpler items, a wash and maybe a wax, and we can call it complete. Thanks again to all our friends that helped so very much in accomplishing all these items, and for just being there, it's what makes our winters so very special.